SVTT Iris · San Vicente — May 2026

PMGD San Vicente de Tagua Tagua · 11.05 MWp · forensic performance & loss analysis
VCOM TNVJVGPM id 1575
team review build

1Loss waterfall — where the energy went

From theoretical (measured POA × capacity) down to actual export. Green-bordered = recoverable; grey = structural/inherent.
reference / subtotal recoverable loss structural loss temperature gain / actual

2Daily energy & performance ratio

Bars = daily export (MWh). Line = PR (%, POA-referenced). Red bars = outage; amber = sensor glitch; dim = weather-limited.

3Inverter imbalance

6 inverters, nominally equal. The “.1” units lag badly → DC-side problem.

4Tracker fleet (173 TCUs)

Each square = one P4Q tracker controller, coloured by mean elevation deviation.
OK <2° 2–10° 10–30° >30° (stuck)

5MVPS / combiner-box (DC input) status

3 inverter stations, 2 inverters + 13 combiner boxes each. Boxes coloured by measured DC-input current on clear days. This is the disconnected-CB view requested.
connected / normal degraded (low current) disconnected (no current)

6Plant single-line — where the faults are

7The May 17–19 outage

~2-day total stop. May 18 logged zero data all day (full SCADA/plant blackout). Root cause not in telemetry — no May O&M report.

8Cross-validation & PR method

Independent checks (all passed)

CheckResult
VCOM export vs GPM meter (May 30/31)identical
Meter vs Σ inverters (month)+0.03%
Stuck trackers: May VCOM ∩ April SCADA
Grid clipping in Maynone (peak 6.35<9 MW)

PR methodology

PR = Egrid / [(GPOA/1000) × Pnom], Pnom=11,048.7 kWp, irradiance = POA (G_M0 = POA CIT2). Temp-corrected with β=−0.34 %/°C (CS7N-655MB-AG), Tmod from sensor.

Measured PR ≈ 65% vs design budget ≈ 89% → ~24 pt real underperformance. Cold month (+5.2% temp gain) means a healthy plant should exceed ~88%.

Caveat: POA CIT2 vs CIT3 diverge 25–47%; CIT3 implies PR>100% (invalid) so CIT2 used. GHI sensors read ~10× low. No plant PR report exists; platform PR channels were dead.

9Fix list — recoverable vs structural

#Issue~MWh/moTypeAction
1DC disconnection + inverter imbalance (MVPS1.1/2.1/3.2; MVPS2 CBs)~130recoverableReconnect/repair CBs & strings on weak inverters
2Tracker fleet — 58/173 misaligned, ~31 stuck~70recoverableMechanical tracker repair (motors/gearboxes)
3Outage May 17–19~40recoverableFind root cause; protection/availability
4Intrinsic system losses (~12%)~115structuralInherent design
5Soilingn/amixedInstall soiling sensor; cleaning cadence
≈190–240 MWh/month recoverable (≈30–38% uplift on May output) — fixing trackers, reconnecting DC sections, and resolving the outage, independent of weather.
Data sources. VCOM REST API (api.meteocontrol.de/v2, system TNVJV) — energy, POA/GHI, 6 inverters, 3 SCB DC-inputs, 173 trackers, ION7400 meter · daily + 15-min, full May 2026. GPM vault dumps (SVI_2026-05-30/31) — meter + 3-inverter aggregate validation. April–May weekly SCADA tracker exports (202604) — independent stuck-tracker confirmation. Engineering refs: P4Q commissioning 00906 (TCU addressing), Tritec layout/block diagram. O&M reports (Reports/SAN VICENTE) are Q1 context.

Tags: figures are measured [M], computed [C] or estimated [E] in the full report. Tracker IDs are P4Q TCU addresses (1–177), not physical TR-001…150 (binding held in the P4Q NCU). Generated from sanvicente-data/out/. Dropbox source untouched (read-only).